ABSTRACT
Well tests exist already for a long time. Since the first oil reservoir was discovered, oil companies have always been keen on estimating reservoir properties such as size. Present day well testing has gone beyond this and its usefulness cannot be overemphasized. This project work is concerned with the use of well testing in identifying well problems. The case under study is the UMU-N2 well of Umusadege field, Kwale. From analysis of the well test data, it was seen that the well had impairment which was due to reduced permeability and thus, required stimulation for improved recovery of the hydrocarbons present. Also, there was high sand and water production which also reduced the productivity of the well.